Vision prototype photo

Vision prototype photo
This is the Vision prototype designed/built by Steve Rahm in USA. and still being supported by Pro Composites Ltd. in USA. The aircraft is a 2 seat side by side, scratch built from a series of manuals. Built entirely of fiberglass and carbon cloth material the builder needs to know or learn some of the easy basics of composite construction. Building began Feb. 1998 in my spare time with 7 years where no building was possible. Building Hours at February 28, 2022: 4248.--------------------------------------------------------------------------------------------------------------------------------Some short videos of flights are at: https://www.youtube.com/channel/UCfxJXIwvmfNlNF3gwplFw7Q

Wednesday, March 22, 2023

Install of a backup Airspeed Indicator and Installation of One way Fuel tank Air vent valves at wing tips.

 March 22 2023

Addition of the backup airspeed indicator is  installed in the panel.  Reasoning for this is in case of the very rare possibility of the main screen going dark.  The glass panel screen has a backup battery which will keep the screen on for 1 hour should ship power be lost.  The backup airspeed indicator would give me airspeed should my main screen be lost during flight.  Landing approach speeds would be readable for a safe landing.




Addition of the One Way fuel tank air vent photo into the wing tips(left side is the same). Below is the right wing tip with the fiberglass  tip sitting on top of the wing.  The blue colored one way air vent is to allow the air to pass freely into the fuel tank but if fuel were to slosh out as far as the vent tube the one way valve will stop it going overboard.  The fuel tank interior has many ribs and anti slosh hinges installed inside the tank minimizing the sloshing of fuel.  The blue foam on the one way valve is now wrapped completely around the valve so there cannot be any metal contact to electrical connections in the wing tip.





Wednesday, January 11, 2023

Modification to Elevator - Adding additional counterbalance lead -

 January 11, 2023

My elevator was static balanced during construction along the hinge line.  Once installed I found them to be tail heavy when all drive tubes were connected.  I  left the lead weight space accesible (removable foam + rib) in case I needed to add additional lead, just behind the original forward lead installed.  A additional 2 pound of formed lead was added to each elevator tip and elevators are balanced up perfectly.  The lead was floxed into place and a 1/4" rib was installed (floxed) along the aft edge of the new lead.






Two layer of bid fiberglass is to be installed to cover the foam.





Wednesday, August 31, 2022

First Flight (Initial Test Results)

 August 31 2022

Some findings after my first flight.  

The airplane flew well and the engine performed very well.  There were some minor issues that presented and will have to be addressed prior to a subsequent flight.

1. After 2 hours of flight slowly decreasing oil pressure presented but cylinder temperatures remained in the green as did the oil temperature.

 Details:  The belly of the airplane was covered in oil which had escaped from the oil separator can overboard exit point.  Three and a half quarts of oil was lost in 2 hours of flight.  This appears to have been because I have the exit tube hanging below the lower engine cowling by 3 inches.  This resulted in  sucking oil out of the low drain back return tube from the engine case.  I have changed the oil exit tube to be only 3/4 inch below the belly skin which is still 2 inches above the lower engine cowling rear lip.    This might have compounded the negative pressure in the tube because it was hanging to low.  I have taken the oil separator completely out of the vent line circuit for now in case it was causing some sort of venturi effect within it's interior.  Now the vent line rises 2" as it exits the engine and drops down to the exit point 3/4 inch below the belly skin. 

2. Bad landing with low left wing caused bending of the pitot tube as it touched the pavement on exiting runway.

 Details:  The pitot tube was bent back into shape and it tested working fine.  A bit of liquid metal was used to cover up the scrape marks and was then filed smooth and surface painted.  The under side of the wing was damaged at this location and the pitot tube mounting nuts had to be lined up and re-bonded.  The skin was punched in a bit and was repaired and resurfaced smooth.

3. Rudder pedal vertical tubes need reinforcing with gussets.

Details:  During my landing and exiting of the runway into the grass my tail wheel went into full swivel turning me left.  I hammered on the right rudder pedal trying to arrest the left turn and partially broke the right rudder pedal.  This again was my mistake as my only steering option at this point would have been to use right brake to arrest the turning.  I have since seen a Service Letter that VANS aircraft had issued to it's owners to re-enforce the rudder pedal vertical tubes with a gusset.  This I have done, as I believe it is a good safety upgrade.


4. Aircraft is flying in a slightly nose heavy attitude with full nose up trim set.  During the test flight I had to hold very slight back pressure on the stick throughout the flight. 

Details:  I am going to add more weight to the elevator counterweight because I found it to be under balanced after installation.  I am also modifying my tailspring by making it longer and with a little more bend.  This will add a bit of weight to the tail and raise the tail for a bit better forward visibility.  If more weight should be needed I have designed it so I can can bolt a piece of lead directly onto the tailspring.


Wednesday, August 10, 2022

First Test Flight

 August 10 2022

Today was the big day for getting the first flight completed.  The object of the flight today is to break in the Lycoming engine as per the Lycoming recommendation for a totally rebuilt engine which was not run in at a shop after rebuild.  The run in of the engine is supposed to be 2 hours of flight at 2450 rpm and leaned properly for the conditions.  During the second hour the rpm's can be varied from 2350 through to 2550 for seating of the rings to the cylinder walls.  Of course this was only if the airframe would fly as expected.  Weather conditions were just perfect with clear skies and no wind.  At 10:00 in the morning I was airborne and completed racetrack pattern flights 1.0 miles (minimum) from the active runway at my local airport.  Temperature was 20 C and flight altitude was at 6500 feet.  

Here is some additional information for those that are building this "Vision" experimental aircraft.  My engine is very similar to the Lycoming O-320 but is a 1960's variant, Lycoming O-340 build by Lycoming specifically for the Navion twin aircraft. (They only manufactured this engine for about 8 years and was replaced by the O-360).   My engine is a totally rebuilt engine with zero time on it.   It has slightly higher compression and cylinder size than the 0-320 and is rated 140 HP.  The engine performed very well and was showing an indicated airspeed of 158 knots.  Compensating for temperature and altitude on this day the true airspeed was 180 knots.  This is right where I was hoping to see  my speeds.

One of my friends agreed to be my safety person to watch over me in case of issues where my wife might have to be notified, thankfully there was no need.  The flight lasted 2.2 hours and was recorded by my Mode S Dynon transponder to FlightAware.  During the complete time of my test flight I was under the surveillance of Calgary Class C airspace radar persons.  The flight went quite well but my landings were very bad, the first a 2 bounce go around the second a 2 bounce go around and the third a 1 bounce that  sent me 45 degrees off runway stopping in the grass.  After 6 years flying my Quickie Q2 I had some ingrained landing habits I needed to get rid of.  In short this was the tendency to keep pulling back on the stick in landing to pin the tailwheel of the Quickie.  This aircraft requires a flatter approach in ground effect to lessen any tendency to cause the airframe to balloon me back up after touchdown.  More details will be given in a upcoming post.




Tuesday, June 7, 2022

Final Inspection of Aircraft by MDRA rep.

 June 7 2022

Today I had the final inspection completed on my aircraft by a MDRA (Minister Deligate for Recreational Aircraft) in Alberta.  I was greeted by a extremely nice fellow Jeff Duchar who flew his own amateur built aircraft down from Red Deer Alberta.  Arriving at my hangar at 0930 in the morning just as planned.  My Inspection took just under 2 hours to complete and I was offered many accolades on my workmanship.  The inspection went very smoothly and resulted in four items to be attended to.  These were two bolts to be changed, 2 cotter pins to be secured better and two placards to add to the interior.  These items were corrected the next morning and my paperwork was on it's way to Transport Canada for review and then mailing out of my new Cof A for this aircraft.  I was so very pleased with the results of todays inspection and the kindness and common fellowship of a like minded inspector like Jeff Duchar.



Tuesday, May 10, 2022

Brake Test and Taxi Test

 May 9 2022

Below are a couple of videos of my first rolling movement under power.




Wednesday, May 4, 2022

First Engine Run

 May 4 2022

Still making progress towards getting my final inspection completed this spring.  I picked my registration letters that I wanted and made up the data plate and mounted it into the VISION.   The Canadian Registration for my airplane is now completed with Transport Canada and I have the C of R in hand with registration C-GVVI.  On May 4th I made the first run up of the totally re-built Lycoming engine and it started up right away.  This I could not be more pleased about as I had replaced the original carburetor and installed a Australian Throttle Body "Rotec" unit.  I only ran the engine for about 3 minutes to make sure oil pressure, fuel pressure and instruments were all functioning.  A few days later I ran the engine again this time to see it get warmed up and then did a very short taxi test to test the brakes and the steering.  It went perfect and total time on the engine was about 15 minutes.  Then a few days later I tied down the tail to a fence post, chalked the wheels and did the Lycoming recommended run up to full power.  Five minutes at 1000 then 10 minutes at 1400 to get the engine oil to  warm up to 120-140.  Then to 1800 RPM and cycle the propeller three times then full power for a maximum of 10 seconds followed by a cool down for about 3 minutes and another full power test for 10 seconds and then cool down and full power a last time.  Such a pleasure to see the engine get maximum RPM of 2700 on each of the full power tests.